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a. Included in digester b. Breakdown not available c. Reconditioned equipment Plug Flow DigestersPlug flow digesters are used to treat with 11 to 13% total solids scraped manure from dairies. Plug-flow digesters are heated, unmixed, rectangular tanks. New waste is pumped into one end of the digester, displacing an equal portion of older material horizontally through the digester, and pushing the oldest material out through the opposite end of the digester. Over the past 4 years, three 1,000 cow digesters have been built in the US by the author’s clients. The digesters are described, benefits enumerated and a summary table allows comparison of costs and benefits. Craven Dairy Farm, Cloverdale, Oregon – 1,000-cow digesterCraven Farms completed a heated, unmixed, plug flow digester sized for the daily manure production of 1000 cows in December 1996. The winter startup was not a difficult problem. The digester performed without incident. The used engine generators presented many challenges and required a lot of small repairs. However, the used generators were $50,000 cost saving over new units. The digester peaked when treating manure from 750 cows on site and 250 cows worth of manure from neighboring dairies. In November 1999 the farm was sold. The owner is expected to move in and begin operations in summer of 2000. The digester produced about $ 24,000 of electricity and $ 30,000 of digester fiber yearly. The value of digested solids is twice the original estimates. The digester eased manure handling and reduced the cost of application. Pathogen concentrations were reduced two orders of magnitudes based on 3 sets of samples. AA Dairy, Candor, New York - 1000 cow digesterAA Dairy Farm built and started up a at their 550 cow facility as a boiler fired system in October 1997. The digester is sized for planned expansion. AgSTAR provided technical assistance in all phases of the project. Issues with New York State Electric and Gas Co. over a used intertie panel previously approved in Pennsylvania delayed engine-generator startup until June 1998. Modifying the previously approved panel to conform to NYSEG wishes cost the owner $21,000. Additional issues have arisen over NYSEG punitive insurance requirements that are being resolved. The digester has operated without problems. The engine has had occasional outages for repair. In total the generator is operating over 90% of the time. The system is currently producing 70 kWh, hot water and about $60/day of digested fiber. Odor has been controlled. The cost of manure application is substantially reduced. Haubenschild
Dairy, Princeton, Minnesota -
1000 cow digester Haubenschild Dairy Farm started up a digester at their 480 cow while concurrently completing their expansion to 1,000 cows completing startup of their generator in October 1999. The major challenge was from the generator company who delayed equipment delivery, hence system startup for months. The utility, Steele-Waseca Cooperative has been a promoter of and asset to the project. The project has been well received and promoted within the state. The dairy has chosen to wait to install a separator to recover solids for resale. The digester has operated without problems. The engine has had occasional outages for adjustment. The generator is operating over 95% of the time. The system is currently producing 85 kWh and hot water to keep the milking parlor warm. Manure handling is much easier for the owner. Table 2 shows the costs and benefits of these three systems. The cost variation between the systems depends mostly on equipment that the farms already owned and the engine-generator. The benefits depend on the value of electricity and the value of byproduct fiber and heat. AA Dairy funding included a $90,000 grant from the local Soil Conservation District to improve manure management with the balance of the cost paid by the owner.
a. Pump and wiring, no concrete b. Reconditioned, used equipment Covered Lagoon DigestersCovered lagoon digesters are most successful in warmer climates south of the Mason-Dixon line. A properly sized lagoon receives dilute either flush or pull plug collected manure and decomposes the material resulting in year round biogas production. Gas production varies seasonally. Barham Hog Farm, Zebulon, NC - 4000 sow farrow to weanBarham Hog Farm has 5 buildings with pit recharge. The farm was built with a single cell treatment and storage lagoon. The project installed a separate covered lagoon prior to the existing lagoon. AgSTAR provided design, installation and troubleshooting support and worked with NRCS to design the lagoon. Lagoon construction began in July 1996. The lagoon cover, 400,000 Btu boiler and a 120 kW generator were installed in December 1996. Biogas use for heating water began in January 1997. Lagoon cover manufacturing problems limited biogas recovery and the production of electricity, however the boiler has operated almost continuously, providing hot water for pig mats under farrowed pigs. The owner was refunded his money and has purchased a new 40 mil HDPE cover. The 18 month average for biogas recovery is 632 m3/d (22,300 ft3/d) of biogas. Much of the year the generator is operated 12 hr/d at up to 90 kW during the daytime and during nighttime 12 hours a boiler operated to produce hot water for Keeping baby pigs warm . Odor is virtually non-existent. Cheng (1999) found that 30% of the total Kjeldahl nitrogen (TKN), 75% of the P and 20% of the K was retained in the covered cell. Cheng (1999) found pathogen reduction to be 2 to 3 orders of magnitude. The farm has been limited to offsetting about $18,000 per year in electricity and about $12,000 per year in propane purchases. The local utility is not in favor of farm cogeneration. However, odor control benefit is very important to the owner because large subdivisions are being built within one mile of the farm. Also, the improved biological stabilization and nutrient mineralization in the digester resulted in the effluent from the storage lagoon containing 60% less nutrients than before. Consequently, the farm manure treatment and nutrient application complies with the 1997 manure management regulations without additional investment. Martin Family Farm, South Boston, VA - 600 sow farrow to feeder pigMartin Family Farm covered the first cell of a two cell lagoon receiving flushed manure in 1993 and began engine-generator operations in spring 1994 with a matching grant from the Southeast Regional Biomass Energy Program (SERBEP). The first cover slowly sank and collected less gas each year. In 1997, Engineered Textile Products of Mobile, AL and Seamens Corporation contributed a demonstration XR-5 modular cover system to replace the original failed cover design. Martin Farms installed the new cover and replaced the corroded lagoon heat loop with radiators. Methane recovery has been continuous throughout the project, though gas use has not been. The farm has produced up to 397 m3/d (14,000 ft3/d) of biogas and 600 kWh/d during the summer. Winter gas production drops off to less than 170 m3 (6,000 ft3/d) and use has been problematic. The farm has planned and purchased a hot water boiler for pig mats under farrowed pigs. A boiler will more closely match the farm labor skill and availability. Odor is virtually non-existent, the effluent is stable and nutrient content of the second lagoon has been reduced substantially. The major benefit to the farm has been odor control and elimination of objections by neighbors. The farm has produced several thousand dollars worth of electricity. A secondary benefit from the two cell approach has been nutrient reduction in the second lagoon and ease of effluent management in sprinklers on fields that are closer to the neighbors than the farm is. Boland Farm, Williamsburg, IA - 2,700 Head Hog NurseryBoland Farm installed a low cost Permalon cover in May 1998 over their manure storage basin to capture odorous gases. The cover is a complete, bank to bank design with trench buried edges. The basin produces combustible methane as predicted. Gas is flared. The cover was designed for owner installation. The owner, one AgSTAR support person and 6 neighbors assembled and installed the cover over a two day period. The owner later installed a flare with solar powered ignitor. Combustible gas is produced and burned in August and September. The lagoon filled for the first time in spring 1999 and was pumped out with a pto pump that was backed down the bank and through a hatch in the cover. Rainfall collected on the cover has been occasionally pumped off. The cover has almost eliminated odor from the basin. The owner states that they are now able to hang the wash outside for the first time in years. Cal Poly University Dairy, San Luis Obispo, CA, 400 cowsThe dairy is located adjacent to the California Polytechnic State University campus in San Luis Obispo, California. The dairy presently milks 180 cows with a total population of over 350 animals. Most of the herd is housed in freestall barns. About 90 percent of the manure is deposited on concrete and flushed with fresh or recycled water to the lagoon. The remaining 10 percent of the manure is deposited in the corrals and is only collected seasonally. Solids are separated from the flushed wastewater prior to storage in a single cell lagoon. This lagoon has a volume of 19,000 m3 (670,000 ft3), which translates to 50 to 90 days of storage, depending upon the water used by the dairy. A new primary lagoon was located next to the existing lagoon, and has approximate surface dimensions of 80 x 65 m (265 x215 ft). The depth varies from 5.2 to 3.7 m (17 to 12 ft) with 2:1 side slopes. In May 1999, the new lagoon was completed with partial cover in place. The gas handling system including gas blower, meter and the flare were installed and operational. Preliminary gas measurements indicate approximately 130 cubic meters of biogas produced daily from the partial cover of less than 50% of the total lagoon surface area. The biogas is being continuously flared and is maintaining a self-supporting flame. The principle benefit to date has been reduced odor and some reduction of nutrients in the storage lagoon water. The university plans to cover the balance of the lagoon surface and install a microturbine to use the biogas to produce electricity. Table 3 summarizes the costs and benefits of the covered lagoons. These projects were completed with some matching funds, but not more than 50%
SUMMARY Ten digesters are reported in this paper. All digesters have started up and functioned well. All have recovered biogas as expected. There have been some modifications to gas uses. Some of the covered lagoon projects have required new floating covers due to materials assembly or cover design problems. Electricity and heat production are direct monetary benefits of the projects. Key non-energy benefits and byproducts from anaerobic digestion of manures such as digested dairy solids, contributed significantly to the desire of farm owners to install anaerobic digesters. Odor control, mineralization of organic nitrogen, weed seed destruction, pathogen reduction and improved manure handling are non-monetizable benefits demonstrated by existing digestion systems. These factors are increasingly important in sustaining farm viability in rural areas and are appreciated and desired by farm owners. ReferencesCheng, J., et al.1999. Evaluation of Alternative Swine Waste Treatment Systems in Comparison with Traditional Lagoon System. In preparation for: Proceedings of the Eighth International Symposium on Animal, Agricultural, and Food Processing Wastes, American Society of Agricultural Engineers, 2950 Niles Rd., St. Joseph, MI 49085, Des Moines, IA, October 9-11, 2000 [1] Mark Moser, Resource Conservation Management, PO Box 4715, Berkeley, CA 94704 Richard P. Mattocks, Environomics, 5700 Arlington Blvd., #17A, Riverdale, NY 10471
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